| Literature DB >> 36236508 |
Waqas Amin Gill1, Ian Howard1, Ilyas Mazhar1, Kristoffer McKee1.
Abstract
Micro-electromechanical systems (MEMS) vibrating gyroscopes have gained a lot of attention over the last two decades because of their low power consumption, easy integration, and low fabrication cost. The usage of the gyroscope equipped with an inertial measurement unit has increased tremendously, with applications ranging from household devices to smart electronics to military equipment. However, reliability issues are still a concern when operating this inertial sensor in harsh environments, such as to control the movement and alignment of mini-satellites in space, tracking firefighters at an elevated temperature, and assisting aircraft navigation in gusty turbulent air. This review paper focuses on the key fundamentals of the MEMS vibrating gyroscopes, first discussing popular designs including the tuning fork, gimbal, vibrating ring, and multi-axis gyroscopes. It further investigates how bias stability, angle random walk, scale factor, and other performance parameters are affected in harsh environments and then discusses the reliability issues of the gyroscopes.Entities:
Keywords: MEMS vibrating gyroscope; frequency modulated; gimbal; mode mismatch; rate integrated; space applications; tuning fork; vibrating ring
Mesh:
Year: 2022 PMID: 36236508 PMCID: PMC9571586 DOI: 10.3390/s22197405
Source DB: PubMed Journal: Sensors (Basel) ISSN: 1424-8220 Impact factor: 3.847
Figure 1Simple depiction of a proof mass vibrating system.
Figure 2Schematic architecture of a single proof mass vibrating gyroscope.
Figure 3Typical one degree of freedom resonator.
Figure 4Response gain decrement of low-quality factor vs high-quality factor sensing response. (a) shows a response for low quality factor and (b) shows a response for high quality factor.
Figure 5Response gain sensitivity in terms of damping effect.
Figure 6Schematic diagram of Draper laboratory’s micromachined gimbal gyroscope.
Figure 7Ni–Fe alloy-based two-gimbal system gyroscope.
Figure 8Study of different shapes of an MEMS vibrating wheel on a gimbal gyroscope. (a) circular (b) square-edge (c) square-vertex (d) hexagon-edge (e) hexagon-vertex.
Figure 9Working operation of a basic MEMS tuning fork gyroscope.
Figure 10Schematic diagram of high Q MEMS tuning fork gyroscope.
Figure 11Schematic representation of the z-axis freestanding gyroscope [43]: 1—External frame, 2—internal frame, 3—drive electrodes, 4—sense electrode, 5—spring beams, 6—support anchors, 7—linear beams, and 8—circular rotating ring.
Figure 12Schematic view of tuning fork gyroscope with anchored diamond coupling method [45].
Figure 13Schematic representation of the basic design of a vibrating ring gyroscope.
Figure 14Schematic demonstration of the operation of a vibrating ring gyroscope.
Figure 15Schematic view of a novel vibrating ring gyroscope developed by General Motors.
Figure 16Schematic view of eight S-shaped support springs in a vibrating ring gyroscope.
Figure 17Schematic view of MEMS double U-beam vibrating ring gyroscope [56].
Figure 18Design of a multi-ring vibrating gyroscope [57].
Figure 19Schematic diagram of novel two-dimensional micromachined gyroscope developed by Fujita et al.
Figure 20Schematic diagram of a dual-axis micromachined vibrating gyroscope.
Figure 21Schematic diagram of dual Foucault pendulum gyroscope. Two Foucault pendulums vibrate in antiphase motion.
Summary of the development of the most common MEMS vibrating gyroscopes.
| Design | Institution | Year | Performance Parameters | Remarks |
|---|---|---|---|---|
| Gimbal | The Charles Stark Draper Laboratory, USA [ | 1988 | - | The first novel design of a micromachined gyroscope was established with no rotating elements. The 350 µm × 500 µm device structure was constructed with a two-gimbal system. |
| The Charles Stark Draper Laboratory, USA [ | 1996 | Sensitivity of 360 deg/h | A vibrating wheel on a gimbal with a given resonant suspended on a Pyrex substrate. The design shows better sensitivity than the previous designs. | |
| Institute of Micromachining and Information Technology, Germany [ | 1999 | Sensitivity of 65 deg/h | The design comprised comb drives, comb electrodes, and primary and secondary oscillatory systems. The gyroscope sensitivity increased with the new innovative design. | |
| University of Hyogo, Japan [ | 2005 | - | The gyroscope consisted of a two-gimbal system that can operate at atmospheric pressure. | |
| Khalifa University of Science and Technology, UAE [ | 2019 | - | Several shapes were demonstrated for the MEMS gimbal gyroscope. A hexagonal structure provides the lowest linear error with a good scale factor. | |
| Tuning Fork | The Charles Stark Draper Laboratory, USA [ | 1993 | Sensitivity of 100 deg/h | Reactive ion-etching fabrication technique used with polysilicon material. |
| Georgia Institute of Technology Atlanta, Georgia, USA [ | 2004 | High quality factors of 81,000 for driving and 64,000 for sensing frequency | High-resolution single-crystal silicon on insulator gyroscope developed with higher sensitivity and higher quality factors. | |
| Shanghai Institute of Microsystem and Information Technology, China [ | 2009 | Mismatch of 0.12 kHz with quality factors of 804 and 789 for driving and sensing frequencies, respectively | Deep reactive ion-etching fabrication technique used for this gyroscope that can operate at atmospheric pressure. | |
| Beijing Institute of Technology, Beijing, China [ | 2016 | - | Developed a levered system for anchored coupling that increased the in-phase sensing frequency by 50%. | |
| Hanoi University of Science and Technology, Vietnam [ | 2017 | Sensitivity of 11.56 mV/deg/s at atmospheric pressure | The proposed | |
| National University of Defense Technology, China [ | 2019 | Bias instability of 0.59 deg/h and angle random walk of 0.04 deg/ | A polygon shape vibration beam gyroscope with more than 100 Hz bandwidth in a scale ±200 deg/s | |
| Chinese Academy of Sciences, China [ | 2021 | Bias instability of 9.27 deg/h and angle random walk 0.923 deg/ | A gyroscope fabricated with 3D wafer level packaging, driving quality factor, and sensing quality factor recorded at roughly 52,000 and 49,300, respectively. | |
| Si-Ware Systems, Egypt [ | 2022 | Bias instability of 5.5 deg/h and angle random walk 0.2 deg/ | Roll-pitch MEMS tuning fork gyroscope developed with in-plane drive mode | |
| Vibrating Ring | General Motors Corporation, Detroit, Michigan, USA [ | 1995 | - | A vibrating ring structure was invented for a vibrating gyroscope with eight support springs. |
| University of Michigan, Ann Arbor, USA [ | 1998 | As low as 0.05 deg/ | A first polysilicon vibrating ring gyroscope was developed with a 30 to 40 µm thick structure. | |
| University of Michigan, Ann Arbor, USA [ | 2002 | A quality factor of 12,000 with 132 mV/deg/s | A (111) single-crystal silicon material was adopted for the gyroscope. The ring radius was 1.35 mm with 150 µm of structural layer thickness. | |
| University of California, Davis, USA [ | 2015 | A quality factor of 80,000 with a resonant frequency of 250 kHz | A disk resonator gyroscope with a diameter of 600 µm was reported that operated at the whole-angle mode operation. | |
| University of California, Irvine, USA [ | 2015 | A quality factor of 100 k with a stable scale factor of 20 ppm | A toroidal ring gyroscope of 1760 µm diameter fabricated with the epitaxial silicon encapsulation fabrication process. | |
| North University of China, China [ | 2017 | Zero-bias instability measured 61.2 deg/h | A new S-shaped support spring was demonstrated for the ring gyroscope. | |
| Khalifa University of Science and Technology, UAE [ | 2019 | - | Two different designs of multi vibrating ring structures were demonstrated to enhance the sensitivity for space applications. | |
| North University of China, China [ | 2019 | Bias instability measured 8.86 deg/h | Double U-beam support springs were introduced to the vibrating ring gyroscope. A deep reactive ion-etching technology is used for microfabrication. | |
| Yangzhou University, China [ | 2020 | - | The attachment of piezoelectric film increases the gyroscopic sensitivity with forced oscillation and parametric resonance. | |
| University of Windsor, Canada [ | 2020 | Simulated resonant frequency of 64.89 kHz and experimental resonant frequency of 64.91 | The rose petal-shaped support springs provided better mode matching between driving and sensing resonant modes. | |
| Beijing Institute of Technology, China [ | 2020 | - | A hinge frame is used with the ring structure. This new design structure provides high linearity and better mode matching. | |
| Zhejiang University, China [ | 2021 | Geometric analysis | Anisotropy of (100) single-crystal silicon affected MEMS gyroscopic properties. | |
| Multi-axis | Himeji Institute of Technology, Japan [ | 1997 | Sensitivity measured at 0.1 mV/deg/s | A novel two-dimensional design with four cantilever beams that were placed above the glass substrate. |
| UC Berkeley, Berkeley, CA, USA [ | 1997 | Angle random walk recorded 2 deg/ | The gyroscope had a 2 µm thick polysilicon disk of 0.3 mm diameter placed 1.6 µm above the substrate and supported by four beams. | |
| Korea Advanced Institute of Science and Technology, Korea [ | 1998 | - | The gyroscope had a polysilicon structure with two suspended plates that vibrated upon electrostatic actuation by comb plates. | |
| National Tsing Hua University, Taiwan [ | 2005 | Sensitivities measured in the dual-axis sense modes, 7.4 fF/deg/s and 19.4 fF/deg/s | A novel dual-axis vibratory wheel gyroscope with three proof masses can measure the two-axis angular rate independently. | |
| University of California, Irvine, USA [ | 2011 | Linear response in the excess of ± 450 deg/s and 100 Hz bandwidth. Driving and sensing quality factors measured 1.1 million | A four-mass MEMS vibrating gyroscope with a 2 kHz resonant frequency was developed with high quality factors. | |
| University of California, Irvine, USA [ | 2012 | The quality factors for driving and sensing more than a million were measured in the range from −40 °C to 100 °C | A four-mass MEMS vibrating gyroscope was developed on the frequency modulation. The frequency-modulated gyroscope showed a great stable response at a different range of temperatures. | |
| University of California, Irvine, USA [ | 2013 | A 1 ppm precision through self-calibration scale factors with temperature changes of 10 °C | A four-mass self-calibration scale factor gyroscope. | |
| University of California, Irvine, USA [ | 2015 | 100 k quality factors in driving and sensing modes at 2.7 kHz operating resonant frequency | Rate-integrating MEMS gyroscope with dual-proof masses. | |
| Korea University of Technology and Education, South Korea [ | 2020 | - | A three-axis single-drive gyroscope was developed with a driving frequency of 25.44 kHz. | |
| Southeast University, China [ | 2020 | Mechanical sensitivity was measured at 1.75 nm/deg/s and the micro coil sensitivity is 41.4 mOe/µm | A dual-mass MEMS gyroscope that operates by electromotive force and sensing scheme comprising differential tunneling magnetoresistance. | |
| Department of Mechanical and Aerospace Engineering, Politecnico di Torino, Italy [ | 2021 | Minimize the cross-coupling between driving and sensing frequency by separate masses for the driving and sensing axis | A comprehensive FEA was conducted on the dual-mass gyroscope for minimizing the mode mismatch. |
Summary of different research group findings of gyroscope performances on temperature characteristics.
| Year | Institution | Design | Temperature Range | Key Findings |
|---|---|---|---|---|
| 2000 | Jet Propulsion Laboratory, USA [ | Silicon cloverleaf structure | −60 °C to +60 °C | Above 20 °C, the resonant frequency and quality factor decreased |
| 2005 | Jet Propulsion Laboratory, USA [ | Post resonator structure | +35 °C to +65 °C | A decrease of 90 mHz/°C of driving and sensing frequency from the specified temperature range |
| 2007 | Chungbuk National University/Samsung Advanced Institute, China [ | Crab-legs design | 0 °C to 150 °C | Frequency shift minimized by design modification; introduced crab-leg suspension gyroscope design |
| 2010 | University of Maryland, USA [ | Tuning fork | −25 °C to 125 °C | 1 deg/s and 1.8 deg/s deviation from 400 to 500 h thermal cycle |
| 2017 | National University of Defense Technology, China [ | Four vibrating masses with an oblique beam | −40 °C to +60 °C | Drive and sense frequency decreased 10 Hz from −40 °C to +60 °C |
| 2017 | Hitachi Research Laboratory, Japan [ | Tuning fork | −40 °C to +120 °C | Design modification decreased the bias instability to 1 deg/h and split frequency less than 2 Hz within the temperature range |
| 2018 | Hitachi Research Laboratory, Japan [ | Tuning fork | Up to 130 °C | 50 mHz split resonant frequency between drive and sense modes up to 130 °C |
Study of the effect of temperature characteristics on frequency-modulated and rate-integrated gyroscopes.
| Year | Institution | Design | Temperature Range | Highlights |
|---|---|---|---|---|
| 2012 | University of California, Irvine, USA [ | Frequency-modulated | −40 °C to +100 °C | High quality factors of one million in both modes |
| 2013 | University of California, Irvine, USA [ | Whole-angle mode | 25 °C to 35 °C | Self-calibration of the scale factor over a 10 °C temperature range |
| 2018 | Tohoku University, Sendai, Japan [ | Frequency-modulated | 25 °C to 75 °C | Scale factor measured −52 ± 136 ppm/°C |
| 2018 | Dipartimento di Elettronica, Informazione e Bioingegneria, Politecnico di Milano, Milano, Italy [ | Frequency-modulated | 25 °C to 70 °C | A stable scale factor with 35 ppm/°C on the temperature range |
| 2020 | Tohoku University, Sendai, Japan [ | Rate-integrated | 20 °C to 70 °C | Achieved excellent stability of the scale factor −1.84 ± 0.62 ppm/°C |
Figure 22Schematic diagram of an octagonal star-shaped vibrating ring gyroscope.
Summary of different mode-matching techniques from some research institutions.
| Year | Institution | Design Approach | Split Frequency | Mode-Match Frequency | Performance Parameters |
|---|---|---|---|---|---|
| 2006 | Seoul National University, Korea [ | Two control loop designs for driving and sensing | 72 Hz | 0 Hz | Improved sensitivity from 0.8 mV/deg/s to 7.5 mV/deg/s |
| 2008 | Georgia Institute of Technology, USA [ | Prefabrication design + phase-locked loop | 2 Hz | 0 Hz | Improved sensitivity from 7.2 mV/deg/s to 24.2 mV/deg/s |
| 2009 | University of Trento, Italy [ | Automatic adaptive control loop feedback | 200 Hz | 1 Hz | Quality factor 150 |
| 2009 | Georgia Institute of Technology, USA [ | Interface architecture CMOS circuit | 12 Hz | 0 Hz | Sensitivity of 88 mV/deg/s and quality factor of 36,000 |
| 2011 | Newcastle University, UK [ | Displacement feedback control system | 1.8 Hz | 0.1 Hz | Bias stability reduced to 0.5 deg/h from 3 deg/h |
| 2012 | Middle East Technical University, Turkey [ | Phase-related automated closed control loop system | 100 Hz | 20 Hz | Bias instability reduced to 0.83 deg/h from 2 deg/h |
| 2013 | Peking University, China [ | A fuzzy algorithm-based automatic control loop system | 6 Hz | 0.32 Hz | Sensitivity 65.9 mV/deg/s and bias instability of 0.68 deg/s |
| 2013 | University of California, Davis, USA [ | Phase-locked loop with proportional integral derivative controller | 135 Hz | <0.5 Hz | 3.29 deg/h bias instability and 60,000 quality factor |
| 2014 | Stanford University, USA [ | Design optimization technique without tuning electrodes | >10 kHz | 96 Hz | A (100) silicon material quality factor of 100 k |
| 2014 | University of Michigan, USA [ | Whole-angle mode birdbath resonator gyroscope | 10 Hz | - | Achieved a stable angular gain and resonant frequency of 10.46 kHz |
| 2015 | Southeast University, China [ | Tuning frequency, quadrature nulling, and forced feedback automatic control loop system | 32 Hz | <0.26 Hz | Sensitivity of 10.9 mV/deg/s and nonlinearity of 0.1% |
| 2016 | Stanford University, USA [ | Differential internal electrodes design | 350 Hz | 0.005 Hz | 4.79 deg/h of bias instability and 0.29 deg/ |
| 2017 | University of Cambridge, UK [ | T-shaped anchor design modification with open loop mode matching scheme | 4.7 Hz | 0.98 mHz | Quality factor recorded at 1.5 million |
| 2018 | Khalifa University of Science and Technology, UAE [ | Octagonal star-shaped anchor design modification approach | 1.184 kHz | 6 Hz | A (100) silicon material with 177 quality factor |
| 2019 | University of Freiburg, Germany [ | Digital mode matching circuit on noise observations | 400 Hz | 7.6 Hz | Increased overall sensitivity and reduced bias instability |
| 2020 | Southeast University, China [ | Automatic mode matching control loop with virtual Coriolis force | 6.27 Hz | <0.1 Hz | Sensitivity increased from 0.226 mV/deg/s to 4.13 mV/deg/s and bias instability reduced to 2.83 deg/h from 3.76 deg/h |
| 2021 | Georgia Institute of Technology, USA [ | Laser ablation algorithm method to minimize mode mismatch | 191 Hz | 12 Hz | Scale factor measured 4.12 nA/deg/s |